Showing posts with label mini mill. Show all posts
Showing posts with label mini mill. Show all posts

Saturday, November 18, 2017

First real part off the mill...

So I've finally got a part to run to completion! It's not the x-axis part I was making last weekend. I decided to give up on that for two reasons (1) it is a large piece and (2) if anything the printed x axis is the least weak part of the system. I have a bunch of aluminum cutoffs I scavenged ( ~ 50mm x 150mm x 5mm) so I made a smaller part. It's a spinning weapon from one of my kids' combat robots, scaled down by 50%.


This lovely weapon is then attached to a 2822 brushless outrunner and spins at about 7k RPM. It slices, it dices, it kicks other bots out of the arena!


Here's the first attempt. First g-code to run to completion! There are four, 1mm high tabs to hold the part to its stock to prevent flyoff. You can see there is a thin layer of aluminum between two of the tabs, clearly the stock is not flat or the head not perfectly trammed. 


The part tore out easily. I used a decomissioned pair of wire cutters to trim the flashing then a rough diamond file. Careful eye can see a fair bit of backlash in the larger holes and a dimple (due to backlash) on the bottom curve.


So back to the machine. Fiddled around with a number of things and found two things I thought were culprits. The first was play in the y-axis - I fiddled around with my printed housing for the motor and the bolts, and they were a bit loose. I did this on purpose at first because when I tightened everything down the axis became very hard to turn, likely because the print is slightly misaligned which shifts the housing around the shaft out of center. I took the housing apart and drilled out the bolt holes a few mm wider so that the print could slide around laterally. This helped quite a bit - I could lock down the print and the tension only increased a little bit over being loosely coupled. Secondly I tightened a few of the set screws in the saddle - again, to the point where it felt a little harder to turn, but not completely locked down. I also slowed down the Z axis a bit - some testing I was doing mid-week showed slips in the Z over time. I wanted to make sure I wasn't driving down the end mill too quickly and either moving the part or sucking the part up.

This one turned out much better. tolerance on the outer holes is ~0.15mm. The interior hole is about 0.05mm average narrower than the CAD. Which may make sense. In Fusion 360 I have the tolerance set to 0.1mm, and when you are adaptively milling out a hole you are essentially milling concentric circles. If you discretize a circle you get a polygon with a lot of sides, which is inscribed the circle, so perhaps this outcome is a-o-k. I need to study a little more to make sure my intuition is correct.


Anyways, super happy to have a part come off the mill. Repeatability in the Z axis is a bit of a concern and rebuilding the Z axis in metal is likely the #1 priority. 

Sunday, October 1, 2017

Mill tear-down

So Robothon was yesterday. My metal combat bots were both 0-2 but neither was demolished; in fact they both still run. The next competition is at the end of January at the Northwest Model Hobby Expo, so I have a solid 3 months and some change to finish the conversion. 

Today I stripped down the table of my mini mill, because the y-axis has always been particularly sloppy ever since I got it. And I figure I should start with a clean, dialed-in machine. After cleaning chips and wiping down the machine I took off the x-axis by spinning the table all the way to the right and then taking off the handle and key. By jamming the table left to right a few times I was able to free the outer bearing and remove the table. The last bearing I took off by placing a crescent wrench against the bearing and then tapping it with a rubber mallet. Now the Y axis is exposed and the culprit became immediately apparent: the nut on the leadscrew is free floating in a slot in the y-axis table and is supposed to be pinned in place by a screw which was loose. Screwing it down and tightening the handle, the slop was instantly gone. Great, but I proceeded to finish stripping it down to clean and oil. Once the table was off I discovered the column was not properly aligned:



I loosened the outer two bolts and took a half-turn off of the center bolt and was able to rotate the column to visual alignment - once I have the table rebuilt I'll use an indicator on a magnetic base to confirm proper alignment. 

I cleaned off all of the packing grease I could find and rubbed everything down with an oily cloth and reassembled the y-axis. I tightened the screw which pins the leadscrew nut and tightened the nut on the handle to a comfortable tension and there was no visible play in the bed - of course once fully assembled I'll verify with an indicator. 


Tomorrow night I'll assemble the x-axis and work on confirming things are nice, smooth and aligned.

more successes

Next thing to do was cut something with multiple depths. Eventually I'd like to make some keychains for gifts and myself and family (wel...